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Energy Savings with High Rate Aeration PDF
Preview Energy Savings with High Rate Aeration
87th OWEA Annual Conference, Mason, OH, Wednesday, June 19, 2013 Energy Savings with High Rate Aeration Mark R. Greene, Ph.D. Senior Technical Director O’Brien & Gere © 2013 O’Brien & Gere 87th OWEA Annual Conference Today’s Presentation Objective Frank E. Van Lare WWTP, Monroe County, NY Oxygen transfer efficiency Aeration upgrade Side-by-side testing Performance and measured savings What these results mean 2 © 2013 O’Brien & Gere Objective Maximizing Energy Saving with Aeration Upgrade Convert surface mechanical (60, 2-speed units) to fine bubble aeration Predicted saving of 7.4 GWh/yr and $550,000/yr Enhance operability and process flexibility Minimal noise emission Maintain compliant plant operations during construction Phased approach with consideration of primary tank improvements 3 © 2013 O’Brien & Gere Frank E. Van Lare WWTP, Monroe County, NY 135/200/630 MGD Treatment Plant Preliminary Treatment (630 MGD) Screen and grit removal Primary Treatment (200 MGD) East/West Clarifiers Secondary Treatment (135 MGD) 20 Aeration Tanks 4 Quadrants of 5 Tanks 6 Final Clarifiers Sludge Thickening 8 Gravity Units Sludge Dewatering 4 Centrifuges 4 © 2013 O’Brien & Gere Frank E. Van Lare WWTP, Monroe County, NY Aeration Tanks High Rate Activated Sludge 1.5-2.5 hours HRT 14 to 18 tanks in service (varies seasonally) Monitor for nitrate and control F:M to minimize 30 manual gate valves 5 © 2013 O’Brien & Gere Frank E. Van Lare WWTP, Monroe County, NY Aeration Basis of Design • Max: 290 MGD Flow • Avg: 150 MGD (PE, RAS, Recycle) • Min: 95 MGD • Max: 180,000 lb/d BOD 5 • Avg: 95,000 lb/d Load • Min: 50,000 lb/d 6 © 2013 O’Brien & Gere Oxygen Transfer Testing Old Aeration Tank Configuration Field measurements Structural integrity Complete mix Oxygen transfer efficiency › 1.8 lb/hp-hr › 61% of clean water (a) © 2013 O’Brien & Gere Aeration Efficiency in High Rate Systems High Rate Systems Low oxygen transfer efficiency Fine bubble has less turbulence Interference of soluble BOD (surfactants) Solution High sBOD gradient Tank configuration © 2013 O’Brien & Gere Improved Oxygen Transfer Efficiency for Fine Bubble Aeration A Solution Add anaerobic selector Modify configuration to plug flow Extend piping Close 2 effluent sluice gates © 2013 O’Brien & Gere Phase 1 Improvements Phasing Aeration Tank Upgrades 10 © 2013 O’Brien & Gere